Application
Cooler ESP of a cement plant located in Cambodia.
Problem
- Unstable operation of controller
- Worn out mechanical parts & misalignment problem
- Worn out original top rapping system, including loose connection, and broken shaft
Solution
The overhaul maintenance & modification works were carried out within 12 days working 2 shifts / 24 hours:
- Design & modification of DE rapping system from top rapping to side rapping
- Supply of new DE frame & installation supervision
- GVC controller installation
- Supply of minor parts such as CP hammer, insulator, etc.
- Installation of walkway
Limitations & difficulties encountered during maintenance:
- Modification work: Due to the alignment of H beam and rapping shaft, the rapping insulator box with dust removal screw could not be installed directly.
Solution: Minor modification of H beams and DE rapping shaft location was carried out.
- Electrical: 1 keypad to control 3 mainboards.
Solution: Use networking connection and apply on/off push button to control the ESP in case the keypad faces malfunctioning problem.






Benefits
No load test was carried out after installation. ESP was operating efficiently with stable performance.
| Field Number | Before (Load Test) | After (No-Load Test) |
| Field 1 | 0kV/146mA (swing kV) | 42kV/678mA |
| Field 2 | 36kV/541mA | 38kV/729mA |
| Field 3 | 55kV/467mA | 42kV/727mA |










